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Steve's Britannia
Harrison M250 Lathe Refurbishment
1. Intoduction    
During a chat round the "Engineers Table" at the Isle of Wight Model Engineers Society one Wednesday, I learnt that the widow of a recently-deceased member of the club was selling the contents of his workshop, in particular a Harrison M250 lathe.. I arranged to go along and view the lathe and, to be honest, it looked about ready for the scrappy. It had been kept in a damp, wooden shed at the bottom of the garden and was covered in rust.
The cross-slide moved but not the carriage and the headstock rotated - just! The owner had been planning on restoring the lathe but never got around to it. Because of it's poor state, it had been advertised on Tony's Lathes for £450. I made an offer on the complete contents of the workshop, whch was accepted, and then the problem of how to move everything had to be solved. The lathe alone was about 600Kg and there was no obvious way to get it up the garden over waterlogged grass and down a set of four steps to the road.
In the end, it came down to stripping the lathe down to it's various components and transportting the items separately back to my own workshop. The tailstock was removed first, followed by the headstock, then the leadscrew and feed shaft. These had to be removed to free the apron gearbox, the cross-slide and the saddle itself. Next the screwcutting gearbox was removed. Even with all this off, it was still too heavy for two guys to shift so the bed was, with some difficulty, separated from the base. The coolant tank and motor were also removed as were any other bits that would lighten the load.
Over the next couple of months all the parts were thoroughly cleaned and de-rusted, then given a couple of coats of enamel paint. A kitchen worktop base was prepared in the chosen position and the process of rebuilding the lathe started by getting the stand into place and the coolant tank refitted, along with the rear guard.
The lathe had a 3-phase motor fitted and an inverter was discovered amongst the bits from the shed but no control panel for the front. While I got an enclosure for the inverter fitted and wired up, a friend designed and made an operator's panel to be fitted later.
The bedway proved to be in good condition, the rust really being no more than staining because of the induction-hardened ways. The bedway was originally set on some sort of putty and this was carefuuly scraped away from the bedway feet. The gearbox was drained and a close inspection of the gears and shaft undertaken but all appeared to be in order. No attempt was made to remove the main spindle because I had no way to accurately rebuild it with the correct pre-loading on the bearings.
Getting the bedway back into position on the stand was a time-consuming job. The feet on the stand were carefully adjusted to give as level a surface as possible and silicone sealant applied around the eight mounting studs. New packing pieces were placed where the old ones had been, pressed in sealant, and more sealant placed around the mounting points. the bedway was then carefully placed over the studs and lowered down onto the packers. Finally, new nuts were run down the studs and the bed lightly clamped to the base. This was left to settle for a couple of days before doing anything else.
Re-assembly was pretty much a reverse of the strip-down. New gaskets were purchased from Colchester Lathe Co and the gearbox refitted to the bedway. Then the headstock was lifted back onto the bedway and bolted down. The coolant tank was fitted with a replacement pump and the drive motor refitted to it's mounting plate.
The saddle was next followed by the apron gearbox and then the feed drive shaft and leadscrew were wangled back into place and the shearpins fitted. During reassembly, all the thrust bearings on the ends of the shafts and the cross-slide leadscrew were replaced
With all the mechanicals back in place, it was time to finish wiring the lathe and my friend brought the user panel along so that we could test it and set the inverter parameters. The panel also held the switches for the light and coolant pump and these were wired up as well. We had to make a couple of minor changes to the panel wiring because of how the inverter was internally connected but after a little tweaking of the settings, everything settled down well.
Following this exercise, I now have a first-class lathe that is much more accurate than my other lathe and it's the first time I've had flood coolant available since I shut my factory 25 years ago. It's a joy to use.
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